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Micro gas turbine performance evaluation.

Thesis (MEng)--Stellenbosch University, 2016.

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Bibliographic Details
Main Author: Oppong, F.
Other Authors: Van der Spuy, S. J.
Format: Thesis
Language:en_ZA
Published: Stellenbosch : Stellenbosch University 2016
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access_status_str Open Access
author Oppong, F.
author2 Van der Spuy, S. J.
author_browse Oppong, F.
Van der Spuy, S. J.
author_facet Van der Spuy, S. J.
Oppong, F.
author_sort Oppong, F.
collection Thesis
dc_rights_str_mv Stellenbosch University
description Thesis (MEng)--Stellenbosch University, 2016.
format Thesis
id oai:scholar.sun.ac.za:10019.1/100232
institution Stellenbosch University (South Africa)
language en_ZA
last_indexed 2026-06-10T12:41:42.083Z
license_str Other — see source repository
provenance_str_mv Harvested via OAI-PMH from SUNScholar — Stellenbosch University Repository
publishDate 2016
publishDateRange 2016
publishDateSort 2016
publisher Stellenbosch : Stellenbosch University
publisherStr Stellenbosch : Stellenbosch University
record_format dspace
source_str SUNScholar — Stellenbosch University Repository
spelling oai:scholar.sun.ac.za:10019.1/100232 Micro gas turbine performance evaluation. Oppong, F. Van der Spuy, S. J. Von Backstrom, Theo W. Stellenbosch University. Faculty of Engineering. Dept. of Mechanical and Mechatronic Engineering. Gas-turbines -- Performance Gas-turbines -- Aerodynamics Gas-turbines -- Design and construction UCTD Thesis (MEng)--Stellenbosch University, 2016. ENGLISH ABSTRACT: The performance of the BMT 120 KS micro gas turbine engine is investigated in this thesis. The study includes component matching of the engine elements using compressor and turbine characteristic maps to analyse the engine’s performance. Analytical and numerical calculations were used to assess the various thermodynamic parameters of the engine and loss of engine power exacerbated by poor performance of the engine components. Engine performance was modelled using commercial simulation software GasTurb and Flownex SE and an in-house one-dimensional code. Using the numerical computations, a component sensitivity and matching analysis was performed for the engine using the various engine components. The theoretical performance of the engine was validated with experimental engine tests. The comparison of engine simulation results and experimental test data showed a consistent trend. A thrust difference of between 0.5% and 6% was achieved between the experimental and simulated results for the baseline engine. The experimental and simulated exhaust gas temperature of the BMT engine showed differences between 1.4% and 6%. Furthermore, a mean-line turbine design analysis was undertaken to study the possibility of improving the performance of the engine’s axial turbine. Simulations that made use of the mean-line turbine predicted a thrust of approximately 190 N and exhaust gas temperature of 993 K at a speed of 120 000 rpm. AFRIKAANSE OPSOMMING: Die werksverrigting van die BMT 120 KS mikro gasturbine word in hierdie tesis ondersoek. Die studie behels onder andere die gebruik van kompressor-en turbinekaarte om komponentpassing van enjinonderdele te doen ten einde die werksverrigting van die enjin te analiseer. Analitiese en numeriese berekeninge is gebruik om die verskillende termodinamiese parameters van die enjin, asook werkverrigtingverliese as gevolg van die swak lewering van enjinonderdele te ondersoek. Die enjinwerkverrigting is gemodelleer met behulp van GasTurb en Flownex SE sagteware, asook ’n in-huis enn-dimensionele kode. Deur gebruik te maak van die numeriese berekeninge is ’n sensitiwiteitspassing analise ook uitgevoer vir die verskillende enjin komponente. Die teoretiese werksverrigting van die enjin is bevestig met behulp van eksperimentele enjin toetse. Die vergelyking tussen die eksperimentele-and simulasie resultate wys ’n deurlopende neiging. ’n Verskil in stukrag van tussen 0.5% en 6% is behaal tussen die eksperimentele en simulasie resultate. ’n Vergelyking van die eksperimentele en simulasie resultate vir die enjin uitlaatgas temperatuur van die BMT enjin het verskille van tussen 1.4% en 6% getoon. ’n Middellyn analise van die turbine is gedoen om die moontlikhede vir die verbetering van die enjin se aksiaalturbine te ondersoek. ’n Analise wat gebruik maak van die turbine se middellyn resultate dui aan dat ’n stukrag van 190 N en uitlaatgas temperatuur van 993 K by ’n rotasiespoed van 120 000 opm behaal kan word. 2016-12-22T13:29:51Z 2016-12-22T13:29:51Z 2016-12 Thesis http://hdl.handle.net/10019.1/100232 en_ZA Stellenbosch University 130 pages : illustrations application/pdf Stellenbosch : Stellenbosch University
spellingShingle Gas-turbines -- Performance
Gas-turbines -- Aerodynamics
Gas-turbines -- Design and construction
UCTD
Oppong, F.
Micro gas turbine performance evaluation.
title Micro gas turbine performance evaluation.
title_full Micro gas turbine performance evaluation.
title_fullStr Micro gas turbine performance evaluation.
title_full_unstemmed Micro gas turbine performance evaluation.
title_short Micro gas turbine performance evaluation.
title_sort micro gas turbine performance evaluation
topic Gas-turbines -- Performance
Gas-turbines -- Aerodynamics
Gas-turbines -- Design and construction
UCTD
url http://hdl.handle.net/10019.1/100232
work_keys_str_mv AT oppongf microgasturbineperformanceevaluation